Getting 1927 Model T Running
Posted: Sat Feb 03, 2024 11:16 am
My father restored the car back in the 60’s and it ran fine for years. He stopped driving it about 30 years ago and I inherited it. I have rebuilt the car myself now, but I cannot get it to stay running. By working the choke, I have been able to keep it running for maybe 5 minutes at a time. My steps to start up are the following:
1. Full choke, no ignition, crank engine over 4 times
2. No choke, 1 turn on the needle, ignition on, push the starter, it fires.
3. Full choke, 1 turn on the needle, ignition on, push the starter, fires and may stay running if I work the choke.
I have a Kingston B1 Gasifier Regenerator Carb on it. This is the carb that was on it when it ran fine for my father. I have tried closing the needle, opening the needle, full choke, no choke, half choke, adjusting the choke action needle on the Kingston, more throttle; less throttle, advancing the spark, etc., etc.
The top unit on the Kingston (mixing chamber?) is getting plenty of fuel. So much fuel that it is pooling up inside of it. This says to me that vacuum is not a problem and that the choke is working. Gas is being sucked up from the lower unit (bowl) through the manifold and into the top unit. However, too little or too much gas is getting from the top unit, through the intake manifold, through the valves, and into the cylinders.
When I did have it running for 5 minutes, it did not sound bad. That being said, the last time I heard a T run was over 30 years ago. Sounded like all cylinders were firing. No misses, clunks, load bangs, backfires, etc., etc.
The following are things that I have done:
1. New valves were installed and ground in.
2. New plugs and wires were installed. Verified all plugs are firing in the proper order and no wires are touching the head.
3. Coils were rebuilt by the Coilman.
4. Compression is a 30 and 40 wet; yes, the piston rings are bad but it should still run
5. At TDC with a leak test I have blow bye on the piston rings which confirms #4 above. No leak at intake, carb, or exhaust.
6. Over 4 gallons of new gas in the tank
7. Refurbished/rebuilt gas tank and sediment bulbs.
8. No aftermarket air filters or fuel filters. (removed it all)
9. All new gaskets on the Kingston B1. (done multiple times)
10. Fished wires and blew out all ports on the Kingston B1. (done multiple times)
11. Float is adjusted properly. Plenty of gas in the bowl. A nice flow of fuel flows out the bowl when I open the valve.
12. Intake/exhaust manifold gaskets – Replaced these twice with two different styles of gaskets. No blow by here so I don’t think this is the issue.
13. Timing – adjusted several times. Full retard set at just past TDC.
14. New gas lines and the lines are fitted to flow downward. No abrupt turns or kinks.
15. Nothing with compression test or leak test indicated a head gasket issue.
16. Gas tank cap hole is not clogged.
Thoughts?
1. Full choke, no ignition, crank engine over 4 times
2. No choke, 1 turn on the needle, ignition on, push the starter, it fires.
3. Full choke, 1 turn on the needle, ignition on, push the starter, fires and may stay running if I work the choke.
I have a Kingston B1 Gasifier Regenerator Carb on it. This is the carb that was on it when it ran fine for my father. I have tried closing the needle, opening the needle, full choke, no choke, half choke, adjusting the choke action needle on the Kingston, more throttle; less throttle, advancing the spark, etc., etc.
The top unit on the Kingston (mixing chamber?) is getting plenty of fuel. So much fuel that it is pooling up inside of it. This says to me that vacuum is not a problem and that the choke is working. Gas is being sucked up from the lower unit (bowl) through the manifold and into the top unit. However, too little or too much gas is getting from the top unit, through the intake manifold, through the valves, and into the cylinders.
When I did have it running for 5 minutes, it did not sound bad. That being said, the last time I heard a T run was over 30 years ago. Sounded like all cylinders were firing. No misses, clunks, load bangs, backfires, etc., etc.
The following are things that I have done:
1. New valves were installed and ground in.
2. New plugs and wires were installed. Verified all plugs are firing in the proper order and no wires are touching the head.
3. Coils were rebuilt by the Coilman.
4. Compression is a 30 and 40 wet; yes, the piston rings are bad but it should still run
5. At TDC with a leak test I have blow bye on the piston rings which confirms #4 above. No leak at intake, carb, or exhaust.
6. Over 4 gallons of new gas in the tank
7. Refurbished/rebuilt gas tank and sediment bulbs.
8. No aftermarket air filters or fuel filters. (removed it all)
9. All new gaskets on the Kingston B1. (done multiple times)
10. Fished wires and blew out all ports on the Kingston B1. (done multiple times)
11. Float is adjusted properly. Plenty of gas in the bowl. A nice flow of fuel flows out the bowl when I open the valve.
12. Intake/exhaust manifold gaskets – Replaced these twice with two different styles of gaskets. No blow by here so I don’t think this is the issue.
13. Timing – adjusted several times. Full retard set at just past TDC.
14. New gas lines and the lines are fitted to flow downward. No abrupt turns or kinks.
15. Nothing with compression test or leak test indicated a head gasket issue.
16. Gas tank cap hole is not clogged.
Thoughts?