Well I got the radiator all cleaned out, pressure tested and installed. No leaks so it was time for a longer test run. The engine started easily, settled down to a nice idle, and things were really looking good. Then all hell broke loose. I noticed an oil leak near the passenger side crankcase arm. It is leaking between the two hogs head bolts at the front and rear of the arm. Not a little leak but a stream the size of a pencil lead. Not a drip drip type of thing but a steady stream. Then I noticed oil leaking out the threads of #1 spark plug. And about that time The front two head bolts started bubbling water... And then the %^$#@ rebuilt starter (I will not say what vendor it came from other than it was not Lang's) started pouring oil out the front of the starter. So it looks like I have a blown head gasket, and I will have to remove the engine to remove the crankcase and see what's wrong with the gasket ??. The crankcase was straightened on a pan jig so I do not have a clue how I could have that bad of a leak. Im not really sure if the oil at #1 plug is oil or oily water. I did every precaution when installing the head gasket and used guide pins to lower the head into place, so that is another "I do not have a clue what could have went wrong.
The bad thing is removing the engine requires removing the steering column, and raising the front of the body as well as all the normal things.
Tomorrow, I plan on running the engine one more time to let it warm up again and give everything one more chance to settle in. That way I will at least have about 15 minutes run time on the engine. Then while I have it open again I can look for any other issues that may have shown up... After that I will drain the water, gas, and oil and make sure every thing is good to set till this fall. I have ran out of time for this year. Its garden and farming time.
On a good note, the engine sounded real good. It starts very easy, and a lot of the time consuming things are already done , So when I do get back to it, I will not have to build and figure out a lot of things. The fan and belt sizes are restored and figured out. The original accessory radiator I wanted to use seems to be working well. , All the intake and exhaust problems are solved, and so on.
I did notice that there is going to be no way in %$#@ to keep the engine clean. That overhead rocker assembly is going to be one oily mess making machine .....

So I guess Ill move into year #7 this fall and see if this thing will ever get finished ..... to be continued ......